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This is the official blog about the development of OctoMY™, the robot platform for you!
2013-07-23
Honda GX25 Update
The Honda GX25 that I un-boxed for quite some time ago has been started and runs great. I have since moved and it is in storage. The plan is to find a suitable alternator for it and also to create a simple ECU that can be controlled from the roboard. To begin with I will most likely just write the ECU as a routine in C on the roboard directly and use one of its many ports to controll a little RC servo on the throttle.
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